The lady and chow took off last night on a mini vacation and left me with the entire day to get this thing running. I spent a ton of time in the garage, but progress seemed slow.. Until it was time to turn the car over.
A Few weeks ago on facebook I entered a draw that Sven was having and won a Treadstone FMIC. So stoked that I was finally able to get it on!
IMG_20180814_000507 by
mason rice, on Flickr
IMG_20180814_000444 by
mason rice, on Flickr
IMG_20180814_000454 by
mason rice, on Flickr
A Project I had a few days ago was painting the FMIC Piping, air intake, and coolant tank. I used VHT Black pearl Engine paint and it turned out really good. Hopefully it lasts. I would love to get rid of the blue greddy Couplers, but thats a project for another time.
IMG_20180814_000526 by
mason rice, on Flickr
For some reason my anxiety was through the roof once everything was ready to go.
*Primed, and turned keys*
*Nothing happened*
*Primed, and turn keys*
*Nothing happened*
I double checked the wiring for the starter and everything looked good. I turned the keys again and nothing! I pulled the plug for the clutch position and ran a wire thinking that it might have been messed up.
*Turned keys*
*crickets chirping*
I hit up nasioc to figure it out. Turns out that at some point the ignition wire for the starter had came up plugged without me noticing. Easy fix and for the last time I turned it over
AND IT STARTED!!. Instantly the first thing i noticed was a high pitch squealing. Spent a few hours swapping clamps, adjusting FMIC Piping and spraying dish soap on the joints. Couldn't track the leak down for the life of me. Well The car is Warm, everything else is functioning as it should, time to take it down the block without a hood and bumper in the typical project car fashion.
This ended in an abrupt halt on the drive way when the hill assist decided to be a untcay. After some stalling, I figured out a terribly inefficient way to unlock the brakes and rolled the car down the drive way in neutral. I think the can be fixed with a simple adjustment. I hit the road to take a quick drive to the end of the street and back. Peak boost was 10psi. I didn't go WOT due to lack of tune for the down pipe and new FMIC, but i needed to function test before booking a tune.
After a bit of reading I came across a similar boost leak issue. Turns out there is a small hole in the Greddy BOV and if the rubber diaphram fails, the hole will leak.
BINGOIMG_20180814_000629 by
mason rice, on Flickr
Air is Squealing its way out of this hole. apparently NRG makes a replacement diaphram that is far superior to the Greddy, But is 50 dollars on amazon plus 30 dollars for shipping.